Now that the saw cut and the splice plates are on, it does not take a lot of force on the beam to get it to this state, but it will not hold it. When I weld on the lower flange steel, that will create the stiffness to hold it. I do not know if Sunline used weld shrink cambering on the top of the I beam frames. I have never seen the top of a Sunline I beam frame rail without the camper on it. I know Artic Fox does and Palomino does on their older Sabre campers. Since the camper is sitting on top of my I beam, I cannot tell. The RV industry is always pushing to use the least amount of weight and materials and in this case, they are forced to use “tricks” to make a thin beam hold the loads. And it seems to work until pot holes come…
To help explain this issue better, here is the frame droop before I started. This 1 3/16” droop will not allow the slide opening in the camper to be square enough to let the slide go in and out.
This is the frame before I did anything. A string pulled down the camper from about 1 foot before the front axle hanger to the rear.
You can see the frame bending down hill
And the 1 3/16 from bottom of frame to bottom of string
Here is where I am with the saw cut fix and the splice plates. I’m at 9/16” droop. The slide will work in this location, but I do not want to leave it this way. My goal is a true square slide opening.
So thinking on this and some calculations, I have come up with early on in the investigation that the back part of the camper from the center line to the slide and from the rear axle hanger to the back wall weighs 1,600lb. 1,500 to 1,600# is also the current force it takes to jack the back of the frame up to hold a square opening from the 9/16” location.
It then dawned on me, what is the natural deflection of this size beam with a 1,600lb load on it? Using standard beam deflection calcs from the steel construction manual, A 105” long cantilevered beam of this size will deflect at the end of it, 0.600” or a little under 5/8” with a 1600 lb point load on the end wall. If we assume the 1,600 lb is evenly distributed along the 105”, the deflection at the end of the beam is only a little over 0.120” or 1/8”. The way the camper is built, it is neither of those extremes, but more loaded something in the middle.
It then occurred to me, this 9/16” I have now, a good part of this is just the raw weight of the cargo and the camper build weight. In order to make the beam lay in a natural resting state without a jack at the end of the frame, I need to unload some weight from the beam? Then weld on the lower flange reinforcements. So I started removing weight.
• Outside the camper, I removed all the cargo in the rear boxes.
• Inside the camper, I moved anything that weighed more than a few pounds from the back of axle area to the front of the camper. Swivel rocker, fire extinguisher, little table etc.
• I removed all the cargo in the storage hole under the slide.
• I estimate this was approx. 300 to 400# of weight
• Removing this weight, reduced the droop from 9/16 to 7/16” or 1/8 less.
While I was gaining, I still needed a lot more. So I removed a good portion of the slide room weight itself from the frame.
• I loosened up the slide mounting brackets and raised the slide to take some weight off the frame rail. This helped a lot.
• Removing this weight, reduced the droop from 7/16” to almost 5/16” or another 1/8 less.
I was gaining but still needed more. At this point the front tire was on the camper bearing full weight of the front axle. The rear axle was loaded, just no tire as I had a wood block and steel shim under the axle seat. This creates leaf spring forces pushing up on the frame. OK, try removing them, so I did.
• Installed a 20 ton jack stand at the front axle hanger area. This is load bearing.
• Removed front tire.
• Removed the rear axle seat shims. Both axles are now hanging free
• Put wood blocks under each axle seat but with an air gap just to prevent shackle flop if the axle is bumped.
• Installed a red bottle jack at the rear hanger to just kiss the hanger for safety, no upward force.
• Installed a jack stand at the rear cargo box frame and shimmed height to just kiss the frame. Not holding load, just there for safety.
• Re-pulled the string. The 5/16” is now at 3/16” droop.
Here are 2 pics showing the setup
Here is the line of site at 3/16”. It is almost totally straight on it’s own.
And a piece of 3/16” square stock about the bottom of the flange
Then I went to the back of the camper and went to lift by hand on the rear bumper. I could with 1 hand lift some of the weight up. So I put a Sherline tongue weight scale under a rear jack and measured the lift force and distance.
The forces and distances are:
• 1/16” = 100# of lift
• 1/8” = 200# of lift
• 3/16” = 300# of lift
I am now close enough that with very little force on the back of the camper lifting, the beam is in its natural resting state for welding on the reinforcements. By picking 100 to 300# of lift I can create a straight frame.
Now the weld sequence on how to make the frame not move from weld shrink. Here is the plan and the order of the welds. Each will area will have dial indicators and putting down a 1” stitch length as a starting place. The indicators will guide if I can make that length longer. After each weld allow the weld to cool to the 100F area. This will take time to weld out, but time I have.
This brings me up to date on the latest activates. Next is more lower flange flat bar to prep and then start the welding process.
Thanks for looking
John